
Here is a picture of the intercooler
cleaning apparatus from the other side.
It would have been so good to show a picture of brilliantly clean copperware inside the intercooler, sadly this is not the case just yet.
Overall, it's fair to say that the whole mechanism worked exactly as planned, that 20 odd litres of solvent went very dirty pretty quickly, except for massive leaking from the seals round the edges.
What impressed me the most, and encourages me to persevere, was the rate of flow of the solvent through the system.
As it turned out, the pump could easily match the pace of the solvent flowing out the bottom of the system - I used 15mm piping (1 1/4 inch I think), except for the pipe from the pump which was thicker.
The pump I used was an old bilge pump, rated at 500 gallons per hour (with no head I presume), with a float switch.
I'll put this first version down to a learning experience, and I learnt a lot in those very few minutes that the system was running:
1) The bolt holes have to be positioned exactly right, else cracking in the perspex will occur.
2) Patience - let the silicone seals dry properly before doing anything, or use proper gaskets.
3) Perspex bends under the slightest pressure, so use ALL the bolt holes (see 1 above then look at
yesterdays picture again).
4) With the system properly sealed I need a separate vent pipe to facilitate filling/draining the system.
5) Test the system with water before using expensive solvent.
So all I've achieved so far was to make an
even bigger mess in the engine room than before. At least it's relatively easy to clean up.
Of course I think the intercooler pipes look somewhat cleaner.
Version two will work out far better. Promise.
Labels: ABB, boat, engine, Intercooler, turbo